Category: electronics


G07 mistakes

The Electrohome G07 is a simple monitor…  At least that’s what I keep hearing and seeing.

As simple as it is however, I have not had a lot of experience with the G07.  The majority of my experience has been with 1990′s computer monitors and more recently 1990′s arcade monitors such as Wells Gardner and similar.  Compared to the later monitors, the G07 is completely foreign.  For instance, the horizontal output transistor is mounted off of the board on a heatsink.  It’s insulated from the heatsink to keep it from grounding out because the outer case of the transistor is one of the conductors BUT, this conductor does need to go to something so Electrohome uses a bracket with a wire on it that the mounting screws go in to.

G07 HOT
The problem I had ran into was that NTE had included additional insulators in their replacement transistor kit.  I had incorrectly assumed that more insulating is better.  The problem being that it broke electrical contact from the heatsink AND the back bracket which resulted in an open circuit, no high voltage and a dead monitor.

This is a cautionary tale.  The last 3 monitors I have not been able to fix and needed additional help on were due to improperly mounted HOT’s.  Some day I’ll learn this lesson.

Another note about the G07, the hot may appear to test as shorted because of an internal diode.  Always make sure to test from the pins to the case.  Testing between the pins looks like a short.

vapor

For months now Vapor Trx has been driving me crazy.  Every time I looked at it I wanted to sort out the issue.  The problem is that sometimes all of the colors were there and it would work great.  Then usually red would flake out and sometimes green.

I had pulled this board out and reworked it over a good bit.  It had a lot of lifted traces from heat issues and other solder issues along with needing a few caps.  I had done all of this, shoved it back in and it worked great for about a day.   I finally got the chance to dig into it a bit more.

I started by re-reworking the neck board since this is the most likely place for a failure with a color channel to occur.  I popped it back in and it was once again fine for a bit and then it died.  I popped it out and felt that there are 3 color driver transistors that looked very suspicious.  Those were the main spots where the traces had lifted due to heat and they all have crappy clip-on heatsinks that were kind of loose.  I decide to see if the part was bad or if I was having connection issues on the PCB.  I decided to swap the red drive transistor with the green one.

When I tossed it back in the machine, it worked perfectly until I came back the next day.  Luckily it was once again missing a color, but this time green.  So now I could be certain that the transistor itself was failing under load.  I stopped by Vecto, grabbed 3 NTE198′s and popped them in.  I tightened up all the heatsinks and fired it off.

I don’t want to jinx it but I’m now pretty certain that this one is fixed.  Hopefully people start playing it now that the screen actually looks good…

si-727r-ds

Well it’s my fault.  I should have known better and checked this but I had tossed in the incorrect horizontal output transistor.  I had purchased a box of 5 replacements off of eBay for a Wells Gardener 25K7401.  That monitor however had a silicon insulator pad that kept the back of the HOT insulated from the heatsink.  The SI-727 however, does not.  When I stupidly installed that part in the unit, it was shorting out and giving me tick-tick-tick noises because the switching power supply was trying to fire up but went into protective shutdown.

Once I fired the monitor up, the picture looked terrible.  Looking into the cabinet though you could tell an amateur did the harness hack.  He twisted wires together and poorly electrical taped them.  This was not the problem but I fixed it.  Ultimately the problem was that the signal ground came detached in the process of fixing the monitor.  For the life of me, I could not find the proper place to attach this wire but ultimately I found one suitable at least.

The monitor still isn’t quite right.  The picture grows and shrinks slightly when going from light to dark scenes(monitor bloom) and the image does not quite fit the screen.  As annoying as this is though, the game is at least playable now.Lessons learned?

Always make sure none of the legs of the HOT have continuity with the heatsink unless of course it’s designed to do so and if you picture every looks inexplicably bad, check your grounds.

Sharp Image SI-727R-DS

IMG_0737

At The Airlock, there is a dead game in the corner called Hyperdrive.  In fact, it’s not just one but two dead games.  It appears that one side of it was dropped on it’s face.  The previous owner probably left it sitting somewhere without the seat portion attached.  If someone bumped it, it wouldn’t take much to knock it over.

When it got knocked over, I believe the monitor was broken.  This theory comes from the fact that the monitors in each side are different.  Not only that, we have an extra monitor chassis board for the side that was not knocked over.  The monitor this game uses is the Sharp Image SI-727R-DS.  The 7 must be the series, 27 is the size, R is RCA tube and DS is dual scan if I’m not mistaken.

At first, the SI-727 seems like a beautiful chassis design.  It seems like it’s everything that any arcade operator could want in an arcade monitor.  It has fairly detailed silk screening on both sides of the PCB, switchable 15K/25K frequency, a nicely made remote board and it’s very easy to remove the chassis from the frame for servicing.

Further investigation reveals some problems however.   I have a SI-727R-DS board sitting here that I have nicknamed clicky.  We tend to nickname monitors with difficult or repeating problems at the airlock.  For instance, we have squishy, which is the radar screen in pod 4…. As you can guess, that one is vertically squished just slightly.  We recapped it, touched up the solder and it was still squished.  I think the problem may be a shorted diode in the vertical drive circuit but we haven’t had time to pull it back out to check.  We also have had other such as blinky, buzzy, etc.

The SI-727 is clicky though.  If I recall correctly, it makes a clicking noise when you fire it up.  This is most likely the power supply continually trying to power up and then power down when it realizes that the horizontal output transistor is shorted.  The question it, what has shorted the transistor?

I’m really not sure yet.  This brings me to some of the problems I have experienced with the SI-727.  First off, it has some nasty trace rot.  The traces are far too happy to badly separate themselves from the PCB.  Usually this problem is indicative of using too high of a heat setting on your soldering iron but I recently upgraded my iron to an extremely bad ass Hakko FX-951.  The heat control on this iron is better than anything I’ve ever used or seen.  All that said, I think these PCB’s just weren’t made well in the first place.  In this picture, you can see the trace side of the board.  If you click on it, look very closely and you’ll see where I needed to lay some solder wick by the horizontal output transistor and use it to beef up the trace.  I’ve had to use this trick from time to time but usually it’s because a previous technician has screwed up the board.  in this case, just the act of removing the HOT tore up two of the pads.

IMG_0736

The other problem I have with this monitor is that I cannot find a service manual and/or schematic for it.  When a problem like this arises, it can be invaluable to refer to a schematic for troubleshooting.  Sharp Image, the company that made this monitor appears to be long since out of business but I used a sneaky trick to find their old site, The Wayback Machine!  Looking through this old site however proved to be a fruitless effort.  In ALL of the archived pages I checked, old and new, the SI-727 schematic was nowhere to be found.   Some forum post mentioned checking the SI-527 manual, which I did, but that was also a fruitless effort.  All of the components seem to have different reference numbers so that’s not going to be especially helpful.

I’m confident that we will get this issue sorted out but it might be tedious without the schematic…

Asteroids Free Play part 1

asteroids

I knew it wouldn’t be long until another weird arcade issue surfaced.  This is one that has been troubling me since I worked on this machine.  The Airlock picked up a non-functioning Asteroids for fairly cheap a short while back.  Round one of fixing led James (with not much help from me) to bad ram chips.  Once he popped those in, the machine seemed to work until a week later when it didn’t.

During that entire week, the machine was left on freeplay as are most of the newest games when they first come into The Airlock while they are still in the functional testing phase.  The game died and so I took the board home and laid a mile of solder on it to fix all the questionable joints.  I also cleaned up and reseated a bunch of shaky looking roms in nasty wiper sockets.

When I popped the board back it, after a little bit of finagling, it fired right up… in German.  Not a problem, we tweaked up the dip switches and it was good to go.  We didn’t notice the latest problem until we tried to switch it off of freeplay mode.  Flipping the switch made the screen change to “1 coin, 1 play”.  Problem is that when you put in a coin, then play a game, after the game is over, both start lights are flashing as if there are credits on the machine.  Because there are.

We’ve had other bigger priorities to deal with so this was back burnered but I was out there tonight and by pure fluke, my dad called me.  I tend to pace around when I talk on the phone so I paced and walked by Asteroids and hit several of the buttons.  No one had played the game today because The Airlock was closed for a private party who was there only for Battletech.  After I hit the buttons, I noticed that the credit lights were now flashing.  Very curious.

I expect that the problem is that something is cross-wired in the coin door/control harness.  For instance, something may not be grounded properly or what someone thought was a ground is actually another control line and they have tied it together.  Kelly suspects that there is probably a short circuit on the logic board itself.  Maybe I got too carried away with fixing those solder joints?  Who knows.  When we figure it out, I’ll post our discoveries.

Freeze Spray vs Donkey Kong

I’ve been spending a lot of my free time lately helping the guys over at The Airlock bring some of their newly acquired arcade games back up to good working order. The majority of the time, monitors are the problem area with these games.

One of the latest ones I fixed was Donkey Kong. It’s an original dedicated Nintendo cabinet from the early 80′s. One of the better looking design schemes out there. In the cabinet is the original Sanyo EZ 20 monitor mounted up on it’s side which is important to note for later…

This monitor had a weird problem. It lost all ability to hold the picture horizontally which appeared as vertical static since the monitor is mounted sideways. The weird thing though was that when you first turned it on, it was fine but then if you rebooted it, this condition existed. Sometimes it went into this condition after many hours of play though as well.p

With monitors, my usual starting point is caps. The electrolytic capacitors in this monitor appeared to be 30+ year old originals. CRT monitors are notoriously hard on caps. These games were only designed to last 2-3 years at the most since in the golden era of arcade, it was unfathomable that anyone would care about a game past that point.

Back to Donkey Kong though. Of course I started with the caps. I figured I had fixed it when I fired it back up to a perfectly clear picture. I turned it off to finish reassembling the monitor and when we turned it on to retest, we found our familiar squiggles.

Kelly, one of the guys at The Airlock, thought this may be a logic board problem in the video circuitry since it was a problem we were unfamiliar with in our experience of fixing monitors. After 20 feet of solder later and many questionable joints fixed on the logic board the problem still remained however.

Enter the freeze spray

Since the problem appeared only after the game warmed up, I figured that we may have a chance to pinpoint the faulty component with the old freeze trick. I grabbed a can of r134a that is on hand there and the little red straw and started blasting while someone watched the screen for me. It didn’t take long since the screen went back to a perfect picture practically on my first spray.

I power cycled the system and luckily the problem immediately reoccurred. We repeated this process, each time being more precise with the can of spray until we finally pinpointed the problem component, a 1/4w 1k resistor. Swapping that out fixed the problem and it’s been rock-solid ever since.

It was interesting to me that a resistor became heat sensitive. I was originally expecting it to be a solder joint, a cap(but they were all replaced) or a heat-sensitive IC perhaps.

After 6 months of talking about it, I finally gave my soldering 101 presentation at Black Lodge Research today.  If you were there or not, there are a few points that I was trying to drive home with this presentation.

  • Wash your hands and beware of lead
  • Clean your tip
  • Lead-free solder sucks ass!
  • Secure your work with fun tak

For those who missed it, sorry.  For everyone else, look forward to a couple of future classes on soldering surface mount devices and another one about making your own circuit boards at home.  Here are the slides and notes from the class:

Soldering 101 Open Office Presentation

Soldering 101 Presentation notes

Thanks to the folks who came out and made this talk fun and also thanks to the folks who dropped money in the donation box to help keep our hackerspace running.

Since I bought my Librettos for $15-$20/ea, I didn’t want to spend $40 on a rebuilt battery so I decided to have my friend James help rebuild a couple of the packs I have.

I have a 2 x 6-cell packs and 1 x 3-cell pack.  I purchased 9 “new” “Sony” 17670′s off of eBay.  I say new in quotes because they were not new when they arrived.  They obviously had been welded previously and someone ground the solder tabs off of them.  Also, we tested all 9 of the cells before we soldered up the pack.  Out of the 9, we found 3 of them at .66-1.30 volts.  When a Lithium Ion cell gets discharged to that point, you can kiss it goodbye.  It’s no longer viable because the chemistry changes and becomes less stable.  Another 3 were in the 2v ranges which may have been recoverable but probably not worth screwing with since it’s still outside of the specified operating range.  The final 3 were in the 3v range which was ok.  4.2v would be fully charged and none of them were anywhere near that.  Not that I’d expect them to be.

I say Sony in quotes because the batteries were counterfeit.  We could tell this because the physical structure of the cells are all slightly different and mismatched.  The blue jackets are printed at a very low quality level and are wrinkled in places where they’ve been improperly shrunk.

Counterfeit batteries are a HUGE problem on eBay.  I firmly believe that probably over 85% of the Lithium Ion batteries on eBay are counterfeit or of inferior/dangerous quality.  Most of them are extremely overrated as well.  For instance, a 18650 cell simply cannot hold 4000MaH.  It’s not physically possible for on of these cells output that much energy without draining it to an unusable state.

Whatever the case, our theory is that we are sending out batteries over to China to be recycled and they are disassembling the battery packs and reshrinkwrapping them and then selling them back to us on eBay.  Not sure if that’s the case with all of it but I’m sure that some of that is happening.

In the picture above, you can see very clearly the example of the wrinkled jackets.  Also, notice the real Sony cells on the right have different/darker colored jackets.

We finished the 3-cell battery up anyways with the 3 half-decent cells we picked from the batch.  I tossed it in my fancy outboard charger that came with one of the laptops and so far so good.  No heat and no smoke.  Time will tell if the rebuild was even worth the trouble.

I have been asked by a LOT of folks which soldering iron I recommend.  To give a little background, I used repair CRT monitors for a living back when A) a monitor was cheaper to repair than replace  B) crt monitors were still in style.  Sure it’s been a while but over the years I’ve used different irons.  At that particular job, I used a Weller solder station.  It wasn’t terrible but I can’t say it was overly impressive either.  It was cheap ($60) and it got the job done.  After that job, I didn’t buy my own solder station for years.  Instead I bought cheapo irons from Radio Shack like it was going out of style.  They used to be about $3 when I started buying them and now they are up to about $9.  These irons sort of got the job done over the years but they had problems.  I’ll just list off some of the top disadvantages that come to mind:

  1. They take forever to warm up to the proper temperature.
  2. They are unregulated so the temperature can be wildly inconsistent.
  3. The metals in the iron and tip are cheap and dissimilar.  After a while the tip will loosen and it will be impossible to properly tighten it.
  4. The plating on the tip seems to be prone to gumming up and eventually becomes impossible to clean.
  5. If you drop the iron on the cord, it will burn through the insulation.
  6. They don’t come with a stand and I consider the ones they sell unsafe.

The main advantage, price, won me over all those years but I’ve rounded up my “collection” of these irons and it amounted to a large pile.  I buy them like screwdrivers and strategically lose them in places where I’d likely remember to look later…

More recently, I’ve finally started soldering surface mount components on a regular basis so I decided I needed something that was regulated at the very least.  Enter the Hakko 936.  The 936 is NOT expensive for a solder station.  In fact, you can get it on Amazon for around $85-$95 typically.  Compared to my old Weller, it feels like a Mercedes Benz of soldering stations if there ever were such a thing.  Instead of my typical conversational review, I will just explicitly list the advantages here:

  1. Heats up in 10-15 seconds.
  2. Indicator light lets you know it’s on.
  3. Temperature is regulated and it bounces back fast when pressed.
  4. Comes with a beefy stand with an integrated sponge to keep the tip clean.
  5. Burn proof wire from the iron to the base unit.
  6. ESD safe. (seems to be, I haven’t fried anything with it)
  7. Light weight iron feels well balanced in your hand.
  8. Tip stays clean for a long time.
  9. Chisel tip included with the iron is very versatile.(for my uses at least)
  10. Don’t need a 15w, 25w and a 40w solder iron to do different jobs.  This one does it all.

There are probably even more advantages that I’m not thinking of but this list is a good start.  Back when I started buying the crappy Radio Shack irons, I didn’t really know any better and soldering stations were still $150-$200 for a professional grade model.  Thanks to global economics, demand and competition though, there are several choices under $150.  Yes, there is also the Aoyue 936 for $50.  I have not used it or compared them side-by-side but I can tell you that the Hakko looks, feels and performs like a professional piece of equipment.  It does what I expect, when I expect it and overall has exceeded my expectations.

By the way, the Hakko(at least mine) is made in Japan if you were wondering.  In the past, when I’ve tried to cut corners by purchasing the knockoff tool, I’ve ended up with something that doesn’t last and is disappointing.  Anyone who has ever shopped at Harbor Freight knows what I mean.  I expect the 936 will be the last soldering station I will ever need.  Now a hot air pencil is a different story ;-)   Beyond the 936 models, there is also the digital readout version of the Hakko solder station but it’s considerably more expensive for something that won’t make your soldering a damned bit better.

I keep my soldering station pegged at 700 degrees.  If you are soldering something more sensitive or more heavy duty, adjust as needed obviously but 700 degrees seems to work well for my purposes.  If you have concerns about this, consult the data sheet of the component you are trying to solder.  Also, Don’t buy this awesome solder station and use crap solder.  Grab a spool of Kester 44 Rosin Core Solder 60/40.  I have a roll that I’ve been using since 2001(it’s dated) and it works great.  The lead free solder is complete and utter garbage in my experience.  It makes for lousy solder joints and is just generally hard to work with.

While you are rounding out your kit, a Flux pen and Chem-Wik desolding wick are both extremely nice to have.  Don’t buy 50′ of Chem-Wik from Amazon though.  They come in 5′ rolls that should be less than $5 or so.  Please feel free to comment on any experiences you’ve had with Hakko or Aoyue gear in the comments.  Happy soldering!

This project was started roughly 8 years ago when the large Boroughs B-7971 nixie tubes were still reasonably priced.  My friend scored these six tubes on eBay for $10/ea.  These particular tubes were salvaged from the ticker boards of the New York stock exchange. The clock uses an older Atmel AVR 90S2331 microcontroller as a CPU.  The code was written in bascom also by my friend after a two-year setback where my wife moved the clock while it was only half assembled and fried the first Atmel chip.  I originally modified my friend’s code in RVK but he decided to gut the code and rewrite it by the time we got around to revisiting this project.  I built the case out of 1/4″ oak that is obviously stained black.  There are no nails in it.  It was done entirely with wood glue and clamps since that’s what I had at the time I started the project.

My friend James painstakingly built the entire circuit on perf board for me.  The tubes are driven directly from 12 TD62084AP 8 channel high voltage driver ICs which are in turn driven by an array of 12 cascaded 74HC595N shift registers.  Other than that, there is a beefy power supply that puts out the 170v and some lower voltages for the logic circuitry.  It uses the 60Hz of the A/C line for a sync source.

I’m very pleased with how the final clock turned out.  It seems to keep the time very well.

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